AAIB investigation to EC135 P2+, G-POLA

Loss of NR control during flight test due to a faulty N2 adjuster, Morpeth, Northumberland, 5 April 2018.

Summary:

During a maintenance flight to adjust engine speed, main rotor rpm varied between its maximum and minimum continuous limits. A mechanical stop within the adjusting potentiometer had failed in such a way that main rotor speed could not be controlled accurately, putting the helicopter at a significant risk. The pilot had not been specially trained to carry out the flight test but his actions in flight prevented rotor speed exceeding its limits and a more serious outcome. The manufacturer and operator have taken safety action regarding the conduct of airborne engine speed adjustments.

Download report:

EC135 P2+, G-POLA 12-19

Download glossary of abbreviations:

Glossary of abbreviations

Updates to this page

Published 24 October 2019