AAIB investigation to RAF 2000 GTX-SE, G-BXDE
Loss of control on takeoff, North Weald Airfield, Essex, 14 September 2018.
Summary:
G-BXDE was being flown for the purpose of revalidating the owner’s gyroplane rating. As the gyroplane became airborne it rolled to the right and turned through 180° before descending back to the ground. It struck the ground on its right side to the right of the runway. The examiner sustained serious injuries.
The investigation concluded that the gyroplane took off with insufficient rotor speed and excessive airspeed. It is possible that the gust lock had been left engaged, restricting the movement of the control stick.
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